Another video update! This was filmed a while ago but I just finally got around to editing it down. I also filmed the method I used to load the back tires with 48 gallons of windshield washer fluid. It was easy!!
The tractor has been running great and has been coming in very handy the last several weeks.
A while back I picked up a new piece of machinery to help with many of our projects. It is not what I was originally looking for. I had been looking for a backhoe attachment for my Kubota tractor. The Kubota B20 was designed to be a TLB (Tractor / Loader / Backhoe) and has a frame integrated quick attach system designed for the matching BT650 backhoe unit. This is more solid and preferable to 3 point mounted units. The added weight due to this frame design makes them surprisingly capable and the backhoe units for them rarely come up for sale.
Loading your tractor tires with windshield washer fluid is an easy upgrade giving more traction, better hill stability, and additional weight / ballast. This is also helps with using a front end loader. I decided to use windshield washer fluid since it is inexpensive, easy to obtain, will not freeze, and will not corrode the wheels like calcium and some of the other wheel ballast options.
First startup after initial 30-minute run-in and head bolts re-torqued. Now starting to apply load to break in the engine and seat the piston rings.
This is the first time the tractor has moved under its own power in many years! Entire chassis has been split, separated, cleaned up, restored and painted.
Also talk about some of the remaining issues that still need addressed in the steering column, and the front gear case on the left side wheel.
I have repaired both of the issues discovered during the engine break-in video. The steering column had way to much play and lifting up on the steering wheel cause it to pop out of place, and the front axle had a major oil leak at the front left hub.
The repair to the steering was much more difficult than I had expected! Instead of being a broken shear-pin like I had hoped, it turned out the input shaft to the power steering box had broken instead of the pin. It was amazing I had any steering at all!
A replacement power steering box from Kubota was over $600, and I didn’t see any used ones available online. A look at the parts tear down showed me that welding to this shaft was likely to be an issue, as it had rubber seals o-rings on the internal worm gear portion. After talking over options with several friends, we came up with the plan to drill a new hole in the shaft. There were a couple hurdles to this.
First – the shaft is hardened. None of the drill bits I had could even scratch this material. After researching online, I read first about ultra expensive carbide bits for hardened steel, and than about people using inexpensive carbide masonry bits the same way. I bought some carbide bits intended for glass and ceramics and they worked great!
I had to remove the top cover to the power steering box for clearance so I taped it all up to keep the metal shavings out of the inside. I then went nice and slow with the smallest bit in the kit, and then stepped up progressively to the size I needed for my through-bolt.
The second issue was that there wasn’t actually enough room on the upper steering shaft for the second hole. This wasn’t too big of a problem though. I just welded on some tabs / ears at the bottom to lengthen it, and then through holed that. This was plain old steel so the welding and drilling went uneventful.
The last hurdle to the repair was that now that I had a hole in each piece, once the power steering box cover was installed there wasn’t enough room to install the bolt! One more hole needed, this time in the cast iron cover for installing the bolt. This one drilled very easy with standard bits as well!
Now I just needed to thread the steering collumn cover back on over the repaired shaft and good to go!
The front axle oil leak was in the swivel point for the left wheel. The bushings in the top knuckle support, which also supports this swivel, were very worn allowing the two sides to have a lot of free play. That movement combined with old dry-rotted oil seals resulted in a very fast oil leak!
I separated the wheel hub gear case from the main axle. I chipped out the old brass bushing from the knuckle support and pressed in a new one. I then removed the two old oil seals. There is a seal in the hub gear case, and another one on the axle arm itself. The oil in the main axle is isolated from the oil in the hub / gear cases on each side. When changing / checking axle oil, make sure you check all three fill points!
I used a trick I had read about for removing both seals since they were in blind holes. I carefully screwed a dry wall screw into the old seal, and then used large vice grips attached to the screw with a hammer to tap the seals out. I tapped the new seals in with a mallet and soft piece of wood to protect the new seals.
I also took the opportunity to replace the torn boots on all three ball joints on the front axle, packing them with fresh grease. Having one of those pop apart with a loaded bucket while on a hill does not sound like fun! And those sort of things have a knack for failing at the most inopportune time!
This is an update to our DIY How To series on How to Build a Large Solar Generator. In this follow up post, I will show you how we can use the quick connects designed into our solar generator to expand both the solar charging capacity, as well as the battery bank for increased run times.
A lot of the feedback was asking how to expand the solar generator to an even bigger capacity system. When I designed the base unit, I wanted it to be very easily expandable using quick connects. There are two areas where we can easily do that with our system:
Spring is knocking at the door, and I am not ready! I have several projects already lined up that I want to use this tractor for, so I need to get it finished up! That said, I still want to paint it since it is disassembled and it is a new skill I want to learn.
I separated all the orange bits from the blue bits, so I could cut down on much of the masking and do a better job at the transitions. I had to figure out a way to lift the loader off without being able to use its own hydraulics (which is how they always seem to be removed on YouTube). I put it in a sling with a ratchet strap and lifted with my engine hoist. I put the rear tires back on the tractor, a rolling hydraulic jack under the front, and rolled the chassis out from under it.
Sidenote – I am not sure why I always end up doing these things in the least efficient order! If I had just removed the loader in the very beginning 1) the tractor would still had both axles and rolled out from under it much easier and 2) removing the front axle / engine would have been so much smoother not working around the loader arms.
Then I welded up some scrap steel to support it using the wedge bolt pin holes. I had to add a strap to keep my support pins from wanting to walk out when working on it, and another to keep the main arm cylinder from wanting to expand & tipping my support stands over.
These machines have a lot going on under those fenders!
Now I am sanding out as many of the blemishes as I can. I have some new decals on order, and hopefully will soon be laying down some nice shiny new paint.
It’s been several weeks since the last update, and I really was hoping the next update would be a running engine. Unfortunately I had a setback on that, which I will get into shortly. This one is going to be a double update!
First up is that the engine and chassis painted up very nicely. I painted the engine and each of the disassembled chassis sections separately, and then again after having them re-assembled. This allowed me to get better coverage on each section, and then the additional coats after assembly took care of the scratches from re-assembly that are bound to happen.
The cherry picker / hydraulic shop crane has proven invaluable for this project. Besides the normal engine pulling / installation, I have been able to use heavy ratchet straps to sling larger assembly’s like the entire front end loader and the front axle / chassis sub-frame. With careful control of each ratchet strap, I was able to pitch the assembly just how I needed and then line up the frame bolt holes for assembly completely by myself. Even with the aid of several big guys, I do not think that could have been done very easily without it!
Once the engine and chassis were all bolted back up, I wanted to test fire the engine before assembling it any further.
I hooked up the minimum connections needed in order to get fuel to the injection pump, and power to the glow plugs and starter. I did not have the radiator installed yet, so I would only be able to run the engine briefly. I also had a scrap piece of wood handy to suffocate the intake with, just in case I did not get all the governor springs inside the injection pump reinstalled correctly.
I bled the air out of each of the injection lines, energized the glow plugs, and cranked it over. Sadly it wouldn’t start. I gave it several attempts and re-bled the injector lines just in case they still had too much air. Eventually I gave up for that night. Later I took the injectors back out for a compression test. I was seeing compression of about 200 psi on #1 and #3, and only 90 psi for cylinder #2. I double checked the valves were adjusted correctly, as that can also give low compression, but all was good there.
I began to suspect the head was cracked from overheating. I know the engine had a history of overheating before it was taken out of service 9 years ago, and likely ran without coolant on at least one occasion due to the cracked T-stat housing I found.
When I had it apart, the cylinder head was warped (about 8 thousands out). I was able to re-surface it myself following YouTube videos, and brought back to within 2 thousands of being flat, which is the workshop manual spec. I also lapped the valves, and was not able to visually see any cracks at that time.
It did not really make sense to have it sent into a shop to be magnafluxed, as the #2 cylinder was pretty eroded, and these heads are cheap enough that if it was cracked a new head from eBay would likely be the same cost or less than repair work on the head. Given that, and the eroded #2 head area, it would not make sense to spend a lot of money repairing this head. But since I didn’t see any cracks at the time, I was willing to invest in a head gasket to give it a shot.
Later after it was all assembled and I had painted the engine, I noticed a crack on the external surface of the head. It appeared to be only in the water jacket area, so I put epoxy on it and tried to forget it was there to ease my mind! But now that my compression is low, the most obvious answer is there were additional cracks that I had not seen.
The good news is I was able to pull the head fairly quickly, without needing to remove the entire engine again.
I stripped the old head and cleaned it back up for a second inspection. I used a brighter light and a magnifying glass this time. I did find there are at least two cracks in the combustion area, between the valve seats and web to the recessed combustion chamber. Here is a full shot of the head, and even knowing where to look in the photo, I can’t see the cracks. You can see the large pitting / erosion of the #2 cylinder though, which is why I didn’t want to invest in any machine shop work for this head.
Here is where I epoxied the external crack I had mentioned in the previous post.
This is the first internal crack I found. It runs well into the valve recess, across the hardened valve seat, along the lower corner of the valley and down into the recessed combustion chamber. This one actually shows a little better in the photo than it does in person. The camera flash must catch it well.
I also discovered this one as well. It crosses the valve seat, and then continues straight into the valley between the ports. It’s harder to see, but its there.
I have purchased some penetrating dye and developer to make finding these kinds of issues at home much easier in the future. I may test it out on this scrap head when it comes in just to see what else shows up!
In the mean time I have ordered a Kumar Bros aftermarket replacement head for this engine. The reviews I could find were mostly positive, and it is quite a bit less expensive than a genuine Kubota one. Hopefully the next update will be a running engine!
I just posted several updates to the Kubota B20 project thread in the forum. I had hoped the next update was going to be of a running engine, but instead it’s more tear down pics and photos of cracks in the cylinder head that I missed the first time around.
Two of the cylinders cleaned up to within spec after surface honing. Cylinder #2 had some very heavy pitting, most likely from water sitting in the cylinder. It needed to be re-sleeved.
I took on re-sleeving the cylinder myself, and it was much more work than I anticipated. I removed the old sleeve by carefully chiseling a slit from top to bottom. I stuck the new one in the deep freezer before installing, but it still took several hours of work in combination with additional ice packs to finally drive it in. If I ever to another one of these, I am definitely going to use dry ice.
Another surprise was to learn that Kubota cylinder sleeves are not bored to final size, due to the amount of force they require for installing. I was not able to find a local machine shop that could do the work that wasn’t already backed up several months. I decided to try boring it myself using a neighbors hone that he was sure could also bore. I was skeptical, but to my surprise, with some patience and frequent bore measurements it worked great! This wasn’t the common inexpensive cylinder hones. It had gear driven racks that applied the pressure to the stones and kept them parallel. After several hours of working with it, I had a cylinder within 3 thousands from top to bottom, and side to side, which is within the factory specs.
After flushing all of the honing grit out of the crankcase really well, I changed out all the crankshaft main bearings and seals. I also polished the crankshaft journals.
I ordered the rebuild kit that included new pistons along with the rings. Here is a shot of the crankcase all cleaned up right before putting the oil pan back on.
Next, I resurfaced the engine head and ground and polished the valve seats. One of the exhaust valves needed replacing due to stem wear.
While putting everything back together, I think I found the cause for the original overheating problems. The T-Stat housing had a crack all the way through, in a location that was almost impossible to see when the engine was assembled. It was a pretty expensive part to replace, so I decided to braze it with Allumiweld rods, which are made for repairing aluminum.
And the final post of updates for now, I have the engine re-assembled and have painted it with primer. It will also be getting a coat of the Kubota Dark Grey Acrylic Enamel before installation.
I am now working on cleaning up and painting the rest of the tractor before putting everything back together again. If anybody knows a good source for Kubota Decals, please let me know!